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Leaky EGR Vacuum Modulator! HELP PLEASE!

Discussion in '1st Gen. Tacomas (1995-2004)' started by tacomatt602, Jun 7, 2015.

  1. Jun 7, 2015 at 8:14 PM
    #1
    tacomatt602

    tacomatt602 [OP] Well-Known Member

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    Matt
    Phoenix, AZ
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    1997 5lug Regular Cab 2.4l
    Doetsch spindles, V6 coils, Fabtech AAL, 4Crawler 2" body lift, Daystar coil spacers, Bilstein 5100s (rear), 15x7 U.S. Wheel Stealth Stars, 225/70r15 Firestone Destination LE2s, '00-04 side mirrors, Prerunner/4x4 grille, Kobalt low-profile toolbox, fucked steering rack D:
    Okay so last weekend, on the drive back down to Phoenix from Payson (bout 85 miles one way), my check engine light turned on. The steep uphills had my little 2RZ working exxxtra hard. I'm assuming that's part of the reason why the light turned on. So once I got back into town, I went to Autozone and had them hook up a scanner to my truck. Turned out to be a P0171 code; lean A/F ratio. Since then, I've replaced my upstream oxygen sensor and PCV valve. Light's still on though. So a couple hours ago I ran that smoke test to check for vacuum leaks and... there's a leak. It's coming from the EGR vacuum modulator. So I linked the intake back up, started the truck and decided to spray some starting fluid at the modulator, expecting to hear a change in idle speed but there was no change. I always thought if you spray starting fluid at a vacuum leak, idle speed would change. :confused:

    So I guess what I'm asking is: should I spend $80 and buy a new modulator? And do you guys have any other suggestions for how to fix that P0171 code?DSC_1442.jpg DSC_1445.jpg
     
    Last edited: Jun 8, 2015
  2. Jun 7, 2015 at 8:50 PM
    #2
    bubbabud

    bubbabud Well-Known Member

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    The scanner that read the code should be able to reset the light and erase the fault code. Also what is that setup you have in place of the intake tube?
     
  3. Jun 7, 2015 at 8:55 PM
    #3
    bubbabud

    bubbabud Well-Known Member

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    Your MAF sensor needs to be in the intake stream to get the proper fuel mix.
     
  4. Jun 7, 2015 at 9:15 PM
    #4
    tacomatt602

    tacomatt602 [OP] Well-Known Member

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    Oh, that was for the smoke test. You basically seal up the intake somehow and blow smoke through it. It was only set up like that for about 30 minutes.
     
    Last edited: Jun 8, 2015
  5. Jun 8, 2015 at 6:36 AM
    #5
    roehoe72

    roehoe72 Well-Known Member

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    I "think" you can clean your egr. But dont quote me. Google it. If not. try a junkyard. Guaranteed it will be less than 80. We all know that risk. Is it the egr or just the gasket for said egr..? Something to check if you already haven't. Good luck and hope this helps. Just curious, how did you perform your leak test.
     
  6. Jun 8, 2015 at 6:50 AM
    #6
    keakar

    keakar Well-Known Member

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    yes it can but they wont do it anymore, least not around here. maybe other states are different but around here they passed a law that said if they reset the code for you then they are responsible for the vehicle so their policy now is check and inform only and never reset anything. if you want to be able to reset it you have to buy your own scanner tool.

    OP - just disconnect the battery for 30 minutes and that should reset the CEL but after doing this everything is reset so it will take about 200 miles or several start and stop cycles running around town for the ECM to adjust the air fuel mix for best performance so it may run rough at first after doing it and you will have to redo your radio presets.

    also that modulator is designed to be open and under that round black cap is an air filter where it draws air in so just because you saw something doesn't mean its bad. look here: http://www.lexls.com/tutorials/emission/egrfilter.html
     
    Last edited: Jun 8, 2015
  7. Jun 8, 2015 at 7:04 AM
    #7
    DesertDigger

    DesertDigger Well-Known Member

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    Got similar code, replaced the actual valve itself cause mine was excessive egr. Meaning valve had build up and wouldn't close. 600 miles later something else with the egr. Assuming now I have same issue you are with the modulator. Honestly it's only really effecting gas mileage.
     
  8. Jun 8, 2015 at 12:22 PM
    #8
    tacomatt602

    tacomatt602 [OP] Well-Known Member

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    Good question, I'll have to look again and see if that's what it is.

    And there's a few ways you can do it, but I decided to blow smoke directly through the intake (helps if the throttle body is wedged open). I just removed the elbow hose connector, sealed up the end of the intake with duct tape, cut a small hole in the duct tape, stuck a funnel through the hole, stuck a small hose through the funnel, lit up a stogie and the rest is history. :p
     
    Last edited: Jun 8, 2015
  9. Jun 8, 2015 at 12:40 PM
    #9
    tacomatt602

    tacomatt602 [OP] Well-Known Member

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    Are you saying that the ECM will adjust to the lean A/F ratio OR that the ECM will adjust the A/F ratio to the correct ratio? Sorry, n00b here.
     
  10. Jun 8, 2015 at 5:32 PM
    #10
    keakar

    keakar Well-Known Member

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    the ECM will adjust the A/F ratio to the correct ratio based on all the sensor readings it gets
     
  11. Dec 18, 2018 at 6:20 PM
    #11
    96_Taco_SC_2.7

    96_Taco_SC_2.7 Member

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    this was really starting to go some where, and then

    I am having similar issues and still need to know if the modulator should leak during a smoke test?
     
  12. Dec 18, 2018 at 6:58 PM
    #12
    cruiserguy

    cruiserguy Well-Known Member

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    The EGR modulator is not airtight. You can pull that top cap off. You'll see a little filter. I would bet smoke would be able to come out of there while smoking it but I haven't smoked my intake before. Check it out and let us know what you think.
     
  13. Dec 18, 2018 at 10:09 PM
    #13
    Glamisman

    Glamisman Well-Known Member

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    the modulator is vented to atmosphere. The lean code is a symptom. It could be as simple a a small exhaust leak.

    I am curious, do you make this run often? The reason I am asking is that if it were me I would run the fuel tank until almost empty then fill up with Chevron gas and make the run and see if a gas with additives that runs cleaner "fixes" the problem. The high end imports I worked on back in the 80's had odd running issues after a while of around town driving and the fix was either dump some techron in the tank, take her on a long multi hundred mile trip or scrape the build up of crap off the intake valves.
     
    96_Taco_SC_2.7 and cruiserguy like this.
  14. Dec 19, 2018 at 12:51 AM
    #14
    Sebz13

    Sebz13 appy polly loggies

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    a dropped one and a high one
    Delete it
     

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